Energy
Waste Solutions
Introduction
The Waste Minimisation Project presents a unique opportunity for Australian
Industry to work Cooperatively on Waste Issues. The collaborative nature
of the Project extends to a commitment by member companies, of disseminating
Case Studies that will benefit Industry as a whole. The following Case
Studies represent a series that showcase successful projects, undertaken
by companies committed to Environmental Waste Management.
Case Study 1:
Arnotts is one of the largest biscuit companies in the
world, with seven manufacturing sites in Australia and the Pacific.
The site at Huntingwood, NSW is a new factory with state of the art
facilities and fully automated production. Even with this site being
of the latest design, there have still been considerable gains to be
made by looking for sources of energy efficiency.
In line with the Arnotts environmental policy to use all resources
efficiently with low amounts of wastage Arnotts has been keen to implement
changes to reduce the use of energy throughout the Huntingwood site.
A range of projects have been undertaken in the areas of reducing gas
and electricity consumption including the reconfiguration of a gas oven
to reduce consumption by over 60%, the reduction in energy used to light
the offices and services tunnels with no effect on the operating environment
and the conversion of the warehouse from LPG to natural gas.
The success of these reduction measures is being capitalised on by
continually looking for new opportunities. Currently they are exploring
the options for co-generation to enable the installation of an efficient
and low cost method of desalination of waste water from the production
processes. They are also monitoring the chilled water tower for the
air-conditioning system to determine the scope of reductions available
in this system.
Lighting of Service areas
With the Huntingwood site being a high consumer of energy, the average
electricity demand per month is around 600,000 kWh, it was envisaged
that there would be a variety of areas in which savings could be demonstrated.
The company set out to identify these opportunities by engaging energy
consultants, their first stop was an audit of the lighting levels in
the factory. This audit highlighted the areas that were typically forgotten
or overlooked and realised that there were significant dollar savings
to be made. This has been demonstrated by the project undertaken to
review the lighting requirements of the service areas and halls. Normally
these areas are frequented only once a week, yet they were being lit
at a constant level 24 hours a day.
The intiatives implemented to reduce the energy consumption in the
service areas and halls consisted of two small but significant modifications
to the lighting system:
· Installation of time delay switches in the service areas.
Allowing automatic switch off after a preset time interval
· Installation of daylight sensors which adjust the lights according
to the available natural lighting
These simple and effective measures resulted in a reduction in the
use of around 260,000 kWh per annum for a capital outlay of just over
$17,000. This investment translated into a payback period of less than
1.5 years.
Case Study 2:
Background
Futuris Brakes International, manufactures friction brake shoes and
disc brake pads for locomotive, freight car and transit applications.
Up until six years ago, Futuris sold product solely to a domestic market.
Since then sales have grown to a point that sees 60% of product exported
to all corners of the globe, including Asia, North and South America,
Africa and Europe. The life expectancy of a typical brake shoe or pad
on a Tangarra, for example is about 3 months. This is still 5-10 times
longer than a comparable cast iron product but necessitates constant
stock replenishment all over the world, to keep up with what is close
to a consumable item. Environmentally conscious production is therefore
a high priority given the amount of dust generated by the manufacturing
process.
The Process
Futuris uses 50 machines throughout its Wetherill Park,NSW site. Compressed
air is connected to each machine to aid in cooling during the production
process or to keep equipment clean and free of dust. Typical of the
machinery in use is:
· Hot Moulding Presses
· Stamping Presses
· Mixers
· Blenders
· Assembly stations
This initiative was selected because compressed air losses could be
readily measured and any improvement would have a significant impact
on the environment whilst reducing production costs.
Also, proposed solutions were not capital intensive and would be easier
to sustain.
Another factor was the non-threatening nature of the project, which
would have minimal effect on disturbing employee relations.
The Initiative
The compressed air system was monitored on a non-production day so leaks
could be easily identified.
Initially, 22 leaks, displaying a range of causes were found across
all machine types.
The causes fell into the following main categories:
· Faulty diaphragms
· Loose nuts on air guns
· Redundant air hoses
An air leak calculator was downloaded from the Sustainable Energy Development
Authority web-site(SEDA - www.seda.nsw.gov.au). This was used to measure
exact losses, savings could then be converted into dollars and the number
of tonnes of CO2 not being released into the atmosphere.
A progressive maintenance program was developed to fix the 22 leaks.
The main feature of the program was its low cost due to the fact that
only minor parts and minimal labour were needed to fix the problem.
The opportunity was also taken to install snap on quick connection
fittings. This facilitated the isolation of machines, where previously
many machines could only be maintained en masse and excessive downtime
was a problem.
Achievements and Savings
Based on the SEDA calculator, annual savings of $43,000 are projected.
More importantly, nearly 500 tonnes of harmful co2 will not end up polluting
our atmosphere.
This is equivalent (and much easier) to removing 110 cars from the
road.
Savings or improvements of a less quantifiable nature are as follows:
· Less wear and tear on the compressor
· Less noise pollution
· A safer working environment, compressed air being a very dangerous
commodity.
Lessons Learned
Many lessons were learned in the course of this project, not the least
being the willingness to address the use of a commodity previously thought
of as an expendable, non-measurable item.
Futuris learnt that:
· Compressed air usage should be classified as a utility and
therefore a cost.
· Substantial savings can be realised without excessive capital
outlay and resources.
· As a project it is easy to measure and fix
· The relative 'cost' of compressed air came as a surprise.
Finally, as energy prices increase, an initiative such as this will
become an even more valuable and non-negotiable undertaking.
Case study 3:
Sara Lee Bakery Australia manufactures and markets a large range of
products for the Retail, Foodservice, Sara Lee Bakery Shops and Export
Markets. Products include; Ice Cream, Cheesecakes, Fruit Pies, Fruit
Danish, Puddings, Cakes, Croissants, Muffins, Quiche and Savoury Bakes.
The Company operates by two main principles: The first is to produce
a range of food products to the highest possible standard and the second
is to be an efficient, low cost producer, so that their products are
priced within the reach of everyone. In this drive to reduce resource
use the company embarked on a range of programs, one of which specifically
examined energy consumption.
Initially a broad review of energy use at the factory was conducted
to identify the areas of high consumption. This process highlighted
the freezers as the main source of energy use and represented the greatest
opportunity to make savings.
Sara Lee Bakery operates from a single site in Australia which is located
just north of Sydney at Lisarow. Initially the raw materials are delivered
to this site and stored in a central holding freezer. During the production
process all products are frozen via a series of spiral freezers which
are then immediately shipped off site to external freezer storage. The
central holding freezer and the five spiral freezers are serviced by
one large Ammonia refrigeration plant.
Changing the temperature without a reduction in Quality
The assessment of the possible savings from the refrigeration plant
led to the set points of this plant to be raised while still allowing
for the core temperature of the product to be within their Quality Assurance
specifications.
The change involved raising the settings from -50 Kpa/ -45oC up to
-37 Kpa/ -42oC.
This simple measure involved no capital outlay and ensured savings
were to be gained immediately.
Other changes have been highlighted by this assessment which will involve
some capital outlay and have a potential to save over $130,000 per annum.
Further Information on the AMC
Industry Waste Minimisation Program and Additional Case Studies may
be obtained by:
Phone: (02) 9209 4051, Fax (02) 9209 4470